A mutex may be configured with rather exotic options such as recursive, unsafe, etc. The availability of these mutex options is controlled by configuation settings. When each option is enabled, additional fields are managed inside of the mutex structure.
pthread_cond_wait() and pthread_timed_wait() do the following atomically: (1) unlock the mutex, (2) wait for the condition, and (3) restore the mutex lock. When that lock is restored, pthread_cond_[timed]wait() must also restore the exact configuration of the mutex data structure if these "exotic" features are enabled.
Now that nxsem_wait_uninterruptible() returns an error when the thread is canceled, new logic is being executed. This revealed an existing error in pthread_cond_wait(). The nature of the error is as follows:
* pthread_cond_wait() must atomically (1) release the mutex, (2) wait on the condition, and (3) re-establish the mutex. Errors can occur on any of these steps. In this case the ECANCELED error was (very correctly) reported by nxsem_wait_uninterruptible().
* However, logic in step (3) had a bug; it re-acquired the mutex, but then a bug in existing logic cause the mutex to be improperly initialized. Essentially, the wrong error status value was being testing. This resulted in a nonsequitar and errors reported by the OS test.
This problem was found by apps/testing/ostest/pthread_cleanup.c
Resolution of Issue 619 will require multiple steps, this part of the first step in that resolution: Every call to nxsem_wait_uninterruptible() must handle the return value from nxsem_wait_uninterruptible properly. This commit is for all remaining drivers in the LC823450 architectures.
Resolution of Issue 619 will require multiple steps, this part of the first step in that resolution: Every call to nxsem_wait_uninterruptible() must handle the return value from nxsem_wait_uninterruptible properly. This commit is for all remaining drivers in the Atmel SAM architectures.
NOTES:
- arch/arm/src/sama5/sam_can.c: Generates several "Mixed case identifier" complaints because definitions provided by header files that are not part of the change.
- arch/arm/src/sama5/sam_pmecc.c: Has two cases of "Mixed case identifies" result within commented out code. There are references to undefined types that might be provided by Atmel logic (Pmecc and Pmerrloc) if it were ever integrated.
Resolution of Issue 619 will require multiple steps, this part of the first step in that resolution: Every call to nxsem_wait_uninterruptible() must handle the return value from nxsem_wait_uninterruptible properly. This commit is for all HCI UART drivers under arch/.
Resolution of Issue 619 will require multiple steps, this part of the first step in that resolution: Every call to nxsem_wait_uninterruptible() must handle the return value from nxsem_wait_uninterruptible properly. This commit is for all I2S/SSC drivers under arch/.
In the sam_usb.c file for these two architectures, the USB suspend() operation is implemented, but never called from anywhere. This logic might be valuable in the future for for now it just causes errors due to the unused static function.
This commit just disables the suspend() logic with #if 0 to eliminate the error. The suspend logic is, however, still preserved in case it is needed in the future.
Resolution of Issue 619 will require multiple steps, this part of the first step in that resolution: Every call to nxsem_wait_uninterruptible() must handle the return value from nxsem_wait_uninterruptible properly. This commit is for all SDIO card drivers under arch/.
The SDIO interface structure includes fields with names like recvR1 and others. These cause "Mixed case identifier" errors from nxstyle in all places they are uses.
This change performs a mass substition of recvR with recv_r to correct this coding standard violation.
Resolution of Issue 619 will require multiple steps, this part of the first step in that resolution: Every call to nxsem_wait_uninterruptible() must handle the return value from nxsem_wait_uninterruptible properly. This commit is for all USB host drivers under arch/.
There is chance pull docker container failure in build jobs,
remove the additional pull docker container step may make it
more stable. Meanwhile, it also saves some time for build job.
Signed-off-by: liuhaitao <liuhaitao@xiaomi.com>
The sub-string MHz is used frequently is pre-processor variable definitions. The section "Lowercase Exceptions" permits reasonable use of lowercase characters in pre-processor variable names and, given the frequency of the use of MHz (no pun intended), it certainly should qualify.
Resolution of Issue 619 will require multiple steps, this part of the first step in that resolution: Every call to nxsem_wait_uninterruptible() must handle the return value from nxsem_wait_uninterruptible properly. This commit is for all SPI drivers under arch/.