95f6c13c61
I still observe data abort crash if I compile the code with optimization enabled. The next steps are to investigate the optimization issue and add Watchdog module. Currently, NSH does not run for a long time ;) arch/arm/src/am335x/am335x_irq.c: Correct interrupt processing routine configs/beaglebone-black/nsh/defconfig: Enable debug compilation options. Otherwise data abort crash is observed arch/arm/src/am335x/am335x_lowputc.c and arch/arm/src/am335x/chip/am335x_uart.h: UART-related cosmetic changes arch/arm/src/am335x/am335x_timerisr.c: Make sure that Timer 1 interrupts are disabled before any access to peripheral registers |
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README.txt |
README ====== This directory contains the port of NuttX to the Beaglebone Black board See http://beagleboard.org for information about Beaglebone Black. This board is based around the TI AM335x Sitara Cortex-A8 CPU. This port was developed on the rev. C of the board: Beaglebone Black (See http://beagleboard.org/black) ITEMS DETAILS -------------------- --------------------------------------------------- CPU 1GHz ARM Cortex-A8 GPU SG530 3D, 20M Polygons/S DRAM 512MB DDR3 800MHz Onboard Storage 4GB, 8bit Embedded MMC, microSD card (TF) slot for up to 32GB Video Output HDMI Extension Interface 2.54mm Headers, 92 pins Network interface 10/100Mbps RJ45 Power 5V, 1000mA Overall Size 3.4" X 2.15" Main features of the TI AM335x Sitara (See http://www.ti.com/product/am3358): CPU - ARM Cortex-A8 - 32KB I-Cache - 32KB D-Cache - 256KB L2 Cache with ECC FPU - NEON SIMD Coprocessor Memory - 176KB of On-Chip Boot ROM - 64KB of Dedicated RAM - 64KB of General-Purpose On-Chip Memory Controller (OCMC) RAM - 16-bit DDR2/DDR3 - Memory capacity up to 8G bits - 8-Bit and 16-Bit Asynchronous Memory Interface with up to Seven Chip Selects (NAND, NOR, Muxed-NOR, SRAM) Boot Devices - NAND Flash - SPI NOR Flash - SD Card - UART TODO: Contents ======== - Beaglebone black Rev.C Connectors - Serial Console - LEDs - Buttons - JTAG - Booting NuttX from an SD card - Configurations Beaglebone black Rev.C Connectors ===================== Serial Console ============== By default, the serial console will be provided on UART0 in all of these configurations. LEDs ==== The Beaglebone black Rev. C has four blue LEDs; three can be controlled from software. Two are tied to ground and, hence, illuminated by driving the output pins to a high value: 1. LED0 GPMC_A5 GPMC_A5/GMII2_TXD0/RGMII2_TD0/RMII2_TXD0/GPMC_A21/PR1_MII1_RXD3/eQEP1B_IN/GPIO1_21 2. LED1 GPMC_A6 GPMC_A6/GMII2_TXCLK/RGMII2_TCLK/MMC2_DAT4/GPMC_A22/PR1_MII1_RXD2/eQEP1_INDEX/GPIO1_22 3. LED2 GPMC_A7 GPMC_A7/GMII2_RXCLK/RGMII2_RCLK/MMC2_DAT5/GPMC_A23/PR1_MII1_RXD1/eQEP1_STROBE/GPIO1_23 4. LED3 GPMC_A8 GPMC_A8/GMII2_RXD3/RGMII2_RD3/MMC2_DAT6/GPMC_A24/PR1_MII1_RXD0/MCASP0_ACLKX/GPIO1_24 These LEDs are not used by the board port unless CONFIG_ARCH_LEDS is defined. In that case, the usage by the board port is defined in include/board.h and src/am335x_leds.c. The LEDs are used to encode OS-related events as follows: SYMBOL Meaning LED state LED1 LED3 LED4 ----------------- ----------------------- ---- ---- ------------ LED_STARTED NuttX has been started ON OFF OFF LED_HEAPALLOCATE Heap has been allocated OFF ON OFF LED_IRQSENABLED Interrupts enabled ON ON OFF LED_STACKCREATED Idle stack created ON ON OFF LED_INIRQ In an interrupt N/C N/C Soft glow LED_SIGNAL In a signal handler N/C N/C Soft glow LED_ASSERTION An assertion failed N/C N/C Soft glow LED_PANIC The system has crashed N/C N/C 2Hz Flashing LED_IDLE MCU is is sleep mode Not used After booting, LED1 and 3 are not longer used by the system and can be used for other purposes by the application (Of course, all LEDs are available to the application if CONFIG_ARCH_LEDS is not defined. Buttons ======= JTAG ==== Booting NuttX from an SD card ============================= These are the steps to get U-Boot booting from SD Card: 1. Stop Beaglebone Black boot process in U-Boot. 2. Insert a FLASH stick into host pc and format FAT32 FS. 3. Copy nuttx.bin into FLASH stick root. 4. Remove the FLASH stick from the host pc. Insert into the Beaglecone Black microSD slot. Load Nuttx into memory and run U-Boot# load mmc 0 0x8a000000 nuttx.bin U-Boot# go 0x8a000000 Configurations ============== Information Common to All Configurations ---------------------------------------- Each Beaglebone Black configuration is maintained in a sub-directory and can be selected as follow: tools/configure.sh [OPTIONS] beaglebone-black/<subdir> Where [OPTIONS] include -l to configure for a Linux host platform and -c means to configure for a Windows Cygwin host platform. -h will give you the list of all options. Before building, make sure the PATH environment variable includes the correct path to the directory than holds your toolchain binaries. And then build NuttX by simply typing the following. At the conclusion of the make, the nuttx binary will reside in an ELF file called, simply, nuttx. make The <subdir> that is provided above as an argument to the tools/configure.sh must be is one of the following. NOTES: 1. These configurations use the mconf-based configuration tool. To change any of these configurations using that tool, you should: a. Build and install the kconfig-mconf tool. See nuttx/README.txt see additional README.txt files in the NuttX tools repository. b. Execute 'make menuconfig' in nuttx/ in order to start the reconfiguration process. 2. Unless stated otherwise, all configurations generate console output on UART0. 3. All of these configurations use the Code Sourcery for Windows toolchain (unless stated otherwise in the description of the configuration). That toolchain selection can easily be reconfigured using 'make menuconfig'. Here are the relevant current settings: Build Setup: CONFIG_HOST_WINDOWS=y : Microsoft Windows CONFIG_WINDOWS_CYGWIN=y : Using Cygwin or other POSIX environment System Type -> Toolchain: CONFIG_ARMV7A_TOOLCHAIN_CODESOURCERYW=y : CodeSourcery for Windows Configuration Sub-directories ----------------------------- nsh: This configuration directory provide the NuttShell (NSH). There are STATUS: Work in progress. Till now it is possible to pass arm_boot(), but Prefetch abort is met when devnull_register() call is done. Have no idea why. I was able to trace down to _inode_search() call. If I put any debug statement like "up_lowputc('0');" right after "desc->node = node;" statement at line 425 the code does not crash.